Need help!!! walkera furious wont bind after update and clear id

Discussion in 'Walkera News and Site News' started by hecp06, Feb 10, 2018.

  1. hecp06
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    hecp06 New Member

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    hey everyone i have a walkera furious 320 c version f3 fc devo 10 remote devo-rx714 osd tilt motors i have updated the fc with betaflight 3.2 put the newest update i lost throttle i had pitch and roll mapping was ok signal lights ok but still no throttle after that i clear the id of the receiver and llost total connection what can i do?????......

     
  2. bjr981s
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    bjr981s Moderator Staff Member

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    Update is not supported. Go back and install original FW and settings.
     
  3. hecp06
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    hecp06 New Member

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    i try but its the same right now i was able connect it but still no throttle i try to put orinal file fro, here but still stuck
     
  4. bjr981s
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    What did you use to install original FW?
     
  5. hecp06
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    hecp06 New Member

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    hey bjr981s thanks for everyhting man all the help got back to the original use the cleanflight took me a bit of time to get the extension but finally got i have other problems lets say motor are getting too hot when im was flight i added the oneshot125 and a current meter that helped alot but the still not flying like before it feel more heavy now and it moves too much in the air i can corrected but there anything i can do to make more still kind of like.i think it might hads to do with my leveling my grounds are not to level lets just say
     
  6. bjr981s
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    What do you mean by this?

    After you updated the FW did you reload the Settings file?
     
  7. hecp06
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    hecp06 New Member

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    it didnt have those feature selected so it was causing my motor to be really hot once i added those feature motors cool again but is still not flying straight im still try to figure out why.
     
  8. hecp06
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    BJR981S hey bud how are u man hopefully everything is ok i find out that my f3 fc was distach from the glue so i just glue it back on i kind have another problem i create it do to my lack of of not knowing the system i try to calibrate the esc and now my motors are staying on and jittering on minimum command.. what can i do?
     
  9. bjr981s
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    Did you re-apply the FW and Settings from the link I gave you? With Cleanflight 1.2.0?

    ESC Calibration is not required. ESC calibration is a requirement if your FC does not know what radio system you are using.

    Walkera FCs are programmed to operate with the default settings of a Devo radio.

    Do not run any Cleanflight utilities or modify any settings. Apply the Default settings file include with the update and don't change anything else.

    Walkera drones do not react well to modification.
     

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